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HomeMy Public PortalAbout01-08-2001 PROCEEDINGS OF THE COMMON COUNCIL OF THE CITY OF RICHMOND,INDIANA,SERVING AS A BOARD IN CHARGE OF THE OPERATION OF THE RICHMOND POWER&LIGHT PLANT MONDAY,JANUARY 8,2001 The Common Council of the City of Richmond,Indiana,serving as a Board in charge of the operations of the Richmond Power&Light Plant met in regular session at 7 p.m.Tuesday,January 4,2000 in the Council Chambers in the Municipal Building in said City.Newly elected Chairperson Phil Dickman presided with the following • Councilmembers in attendance:Howard"Jack"Elstro,Bruce Wissel,Karl Sharp,Bing Welch,Sarah"Sally"Hutton, Paul Combs and Larry Parker.Etta Lundy was absent.The following business was conducted: ROLL CALL Nine present. - APPROVAL OF MINUTES The minutes of the meetings of December 18,2000 were unavailable. APPROVAL OF BILLS,INVESTMENTS AND TRANSFERS Upon recommendation of the Finance Committee,Councilmember Hutton moved to approve the following bills for payment,seconded by Councilmember Wissel and by unanimous voice vote the motion was carried. Bills Already Paid: Payroll and Deductions $253,935.70 Investments Purchased From: Cash Operating Fund Bond Sinking Fund Utility Bond Reserve Fund Depreciation Reserve Fund 91,000.00 Insurance Reserve Fund Consumer Deposit Fund Cash Reserve Fund 181,875.00 Group Insurance Fund Total Investments $ 272,875.00 Transfer from Cash Operating Fund to: Cash Reserve Fund for Payment To City in lieu of taxes Transfer from Cash Operating Fund to: Depreciation Reserve Fund For Property&Plant Transfers from Depreciation Reserve to: Cash Operating Fund Transfers from Consumer Deposit to: Cash Operating Fund . Transfers from Utility Bond Reserve Fund to: Bond Sinking Fund Transfers from Cash Operating to: Interest and Bond Principal Bond Sinking Fund Cash Reserve Fund Utility Bond Sinking Fund Depreciation Reserve Fund Insurance Reserve Fund Consumer Deposit Fund Interest and Bond Principal End of Month Petty Cash Revenue Bonds Interest Coupons Redeemed Interest Coupons Redeemed Bond Coupons Miscellaneous Prepaid Invoices $ 206,330.75 Total Prepaid Invoices 733,141.54 Total EFT/Direct Deposit of Payroll: (76,870.81) Total Prepaid Invoices: 656,270.73 Total EFT Transfers: 450,237.24 ' Total Prepaids plus EFT Transfers: 1,106,507.97 Total Bills Not Paid: 619.681.94 Grand Total of Bills to be approved: $1,726,189.91 ' RP&L Minutes Cont'd January 8,2001 Page 2 REMARKS BY CHAIRPERSON Chairperson Dickman stated that the committees would remain the same for 2001. UNFINISHED BUSINESS There was none. STREET LIGHT COMMITTEE REPORT Councilmember Elstro said there was no report. REPORT BY GENERAL MANAGER General Manager David Osburn said the bids for the pumping re-circulation system for the Zero Discharge Project had been reviewed and recommended that Tramco of Indianapolis be awarded the bid for$213,564.He explained that the amount budgeted had been$190,000 but gave several reasons for recommending the bid.Councilmember Welch moved to approve,second by Councilmember Wissel and the motion was carried on a voice vote. Osbum requested authorization from the Board to repair the Boiler Feed Pump Element as pre-approved in the 2001 Expense Budget.He said it was a maintenance item at the Whitewater Generating Station at a cost of$27,900. Councilmember Wissel moved to approve,second by Councilmember Sharp and the motion was carried on a voice vote. Osburn informed the Board about the transmission line rebuild,giving the background as it was included in the Capital Budget.He said the Greenville Line at the North West 11th Street Substation is two miles in length and would handle the additional load in the Northwest area at a cost of$700,000 and the Highland Transmission Line would run about $450,000. In his General Report,Osbum said that the prolonged cold weather had created a coal shortage,however,it had not affected RP&L. He also mentioned the high gas prices,noting that there had been no increase in the electric because the bulk of the generation of electricity is by coal.He added that the cost of electricity had gone up about 3 percent over last year but that is the normal course. He mentioned at on December 18,2000,RP&L had set a new peak at 9 a.m.of 156 megawatts,up one megawatt from the prior peak of 155. Osburn also gave an update on the maintenance at the Williamsburg Substation at North West 5th Street which feeds mostly industrial,noting about$70,000 in repairs. NEW BUSINESS There was none. ADJOURNMENT There being no further business,on a motion duly made,seconded and passed,the meeting was adjourned. Phil Dickman,Chairperson ATTEST: Norma Schroeder,Clerk