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HomeMy Public PortalAbout08-18-1997 PROCEEDINGS OF THE COMMON COUNCIL OF THE CITY OF RICHMOND,INDIANA,SERVING AS A BOARD IN CHARGE OF THE OPERATION OF THE RICHMOND POWER& LIGHT PLANT MONDAY, AUGUST 18,1997 1 The Common Council of the City of Richmond, Indiana, serving as a Board in charge of the operations of the 2 Richmond Power & Light Plant met in regular session at 7 p.m. Monday, August 18, 1997, in the Council 3 Chambers in the Municipal Building in said City. Chairperson Bing Welch presided with the following 4 Councilmembers in attendance: Howard "Jack" Elstro, Etta Lundy, Bruce Wissel, Sarah "Sally" Hutton, Geneva 5 "Gene"Alen,Alan Stamper, Bob Dickman and Larry Parker. The following business was had to-wit: 6 7 APPROVAL OF MINUTES 8 9 The minutes of the meeting of August 4, 1997 were approved on a motion by Councilmember Hutton,second by 10 Councilmember Allen and the motion was carried on a unanimous voice vote. 11 12 APPROVAL OF BILLS, INVESTMENTS AND TRANSFERS 13 14 Upon recommendation of the Finance Committee, Councilmember Hutton moved to approve the following bills for 15 payment,seconded by Councilmember Allen and by unanimous voice vote the motion carried. 16 17 Bills Already Paid 227,879.65 18 Payroll and Deductions 19 20 Investments Purchased From: 21 Cash Operating Fund 22 Bond Sinking Fund 23 Utility Bond Reserve Fund 24 Depreciation Reserve Fund 25 Insurance Reserve Fund 26 Consumer Deposit Fund 27 Cash Reserve Fund 28 Group Insurance Fund 29 30 Total Investments 31 32 Transfer from Cash Operating Fund to; 33 Cash Reserve Fund for payment 34 to City in lieu of taxes 35 36 Transfer from Cash Operating Fund to; 37 Depreciation Reserve Fund 38 for Property&Plant 39 40 Transfers from Depreciation Reserve to: 41 Cash Operating Fund 42 43 Transfers from Consumer Deposit to: 44 Cash Operating Fund 45 46 Transfers from Utility Bond Reserve Fund to: 47 Bond Sinking Fund 48 49 Transfers from Cash Operating to : 50 Interest and Bond Principal 51 Bond Sinking Fund 52 Cash Reserve Fund 53 Utility Bond Sinking Fund 54 Depreciation Reserve Fund 55 56 Insurance Reserve Fund Consumer Deposit Fund 57 Interest and Bond Principal 58 End of Month Petty Cash 59 Revenue Bonds 60 Interest Coupons Redeemed 61 Bond Coupons 62 Miscellaneous Prepaid Invoices 63,867.52 63 Total Prepaid Invoices 291,747.17 64 Less EFT/Direct Deposit of Payroll (49,568.53) 65 Total Prepaid Invoices 242,178.64 Total EFT Transfers 68,383.86 Total Prepaids plus EFT Transfers 310,562.50 Total Bills Not Paid 489.600.71 Grand Total 800,163.21 I • . RP&L Minutes Cont'd August 18, 1997 Page 2 1 REMARKS BY CHAIRPERSON 2 3 Chairperson Welch said he will be getting a revision in the schedule for this weekend for the interviews for the 4 candidates for the general manager's position. He added that there would be no board involvement until Saturday 5 morning. 6 7 He brought the Board's attention to a couple of articles in the August 10 issue of the Palladium-Item dealing with 8 special interest groups showing interest in the deregulation bills in the legislature. He also commented on an 9 article in the I.M.P.A. newsletter which mentioned legislation. 10 11 He said an announcement will be forthcoming about a working executive session, working around budget 12 hearings in the Committee of the Whole meetings, to schedule talks relating to the quotations received tonight 13 about the boiler retubing. 14 15 UNFINISHED BUSINESS 16 17 There was none. 18 19 STREET LIGHT COMMITTEE REPORT 20 21 MISCELLANEOUS BUSINESS 22 23 There was none. 24 25 REPORT BY GENERAL MANAGER 26 27 General Manager Irving Huffman provided the publisher's affidavit for the ad about the bids on the maintenance 28 work on Unit No. 1 which appeared in the Palladium-Item August 7 and 14. Councilmember Parker moved to 29 accept the proof of publication, second by Councilmember Wissel and the motion was carried on a unanimous 30 voice vote. 31 32 The first bid opened by Huffman was from D.W. Riley Inc.,which he said were the manufacturers of the boiler. He 33 explained the bid request was for the material and installation and the third was for a joint furnishing of material 34 and labor. He said Riley's bid was to replace the steam generator section of the boiler tubes, stating that the 35 specifications had been drawn up by Black&Veach, adding that they evidently did not follow instructions and 36 several things were missing. He said Item A was for 534 boiler bank tubes at a cost of$165,527; Item B for 27 37 rear wall tubes for$23,632; Item C for 56 low temperature super heat elements at$209,940; Item D for 56 high 38 temperature super heat elements at$164,091;Item E,supply all necessary refractory and baffles for a budget 39 quote for a lump sum of$10,000.He said this bid would have to be tabulated and checked for the missing items. 40 41 The bid made by Asea, Brown Bavaria(A.B.B.)gave a lump sum price replacement tubes at a cost of$596,630;a 42 lump sum installation at$764,860;and the entire package at$1,390,430. He added that some options were 43 included. 44 45 A bid made by Kennedy Tank&Mfg. Co.of Indianapolis was for a lump sum replacement of the tubes at 46 $534,957; installation at$849,622;and a total at$1,384,579. 47 48 Councilmember Wissel moved to refer the bids to the general manager for tabulation, evaluation and 49 recommendation,second by Councilmember Hutton and the motion was carried on a unanimous voice vote. 50 51 Councilmember Stamper stated that two meetings ago he had brought up the tubing project and had asked for a 52 copy of any long term strategic plan and had been notified that the Board was going to get a presentation on 53 these things but he expressed a desire to have the numbers before the meeting so he could be prepared to ask 54 questions. He also said he would like to have a list of the age of the key components within Unit No. 1 so the 55 Board could have some record and know how to plan and maintain those. 56 57 Huffman responded that the information will be presented at the special meeting by representatives of I.M.P.A. He 58 said they are going to present the number of outages in the boiler over the past two years and going into how 59 much money was spent just on regular maintenance. He added that what is being done is a normal step in 60 keeping a power plant going, noting that when you are operating a$50 million piece of equipment, repairs are 61 going to cost some money. 62 63 Chairperson Welch stated that RP&L is currently on a five-year major maintenance schedule and there is an 64 annual down outage so minor maintenance can be done. He said it can be called a strategic plan or just policy, 65 but it is a schedule that has been in effect for years. RP&L Minutes Cont'd August 18, 1997 Page 3 1 Chairperson Welch said to predict the replacement of a turbine or generator itself is difficult. He added that these 2 things will be presented at the meeting and he felt it was proper that all of the Board members hear the 3 information at the same time and then it can be discussed. Councilmember Allen asked if the information will be 4 written and Huffman responded that there will be all types, presented as one packet.Councilmember Allen then 5 said if it is going to be presented in written form she saw no reason why Board members could not have it ahead 6 of time, adding that it is difficult to absorb if they get it right before the meeting. Huffman said he will send what 7 information RP& L has at that point and he invited the Board's consultant to sit in and review the information and 8 if that consultant has some questions he or she would like to have addressed he would also like to have those 9 ahead of-time. 10 11 Councilmember Stamper said the reason he did not bring this up before was because he was never worried about 12 it because of the LEBS project,then,when that evaporated, he was aware the Board never talked about tubes 13 and he wondered how much of the strategic plan was built on LEBS. He said he wanted to talk about what the 14 effect was going to be in not getting LEBS on the future of the generation of the utility and the cost efficiency. He 15 added that he just wanted to clarify that. 16 17 Chairperson Welch said RP&L would have built a whole new unit with the LEBS project, but what has been done 18 is that the five-year cycle of the maintenance of the No. 1 Unit has been held up and because of not getting the 19 LEBS project wrapped up, next year the No. 1 Unit will be down for the major maintenance schedule. He said that 20 is the four to six-week outage that Huffman mentioned. Chairperson Welch stated that the strategic plan is clear in 21 the minds of RP&L and this Board and if it is to remain a low cost generator of electricity then it will fulfill the goal 22 of low cost generation. 23 _ 24 ADJOURNMENT 25 26 There being no further business,on a motion duly made,seconded and passed the meeting was 27 adjourned. 28 29 30 31 32 33 34 Bing Welch, Chairperson 35 36 37 38 39 ATTEST: 40 Norma Schroeder, Clerk 41 42 43 44 ' 45 46 47 48 49 50 51 52 53 54 55 56 57 58 59 60 61 62 63 64 65